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HomeMy WebLinkAboutBOA Add'l Items 2-26-15 Earl McMillin /Tetra Tech Report0 Earl McMillin P.O. Box 1086 Cape Canaveral, Florida 32920-1086 (321) 453-0429 emcmillinidPvahoc.coni 21 February 2015 Highlighting and underlining have been placed on the Tetra Tech Memorandum for convenience to point out items pertinent to the Cumberland Farms request. TETRA TECH MEMORANDUM To: Mr. Jeff Ratliff Public Works Director City of Cape Canaveral From: Mr. Brian Foulkes, P.E. Mr. Stephen Glatthom, P.E. Tetra Tech Subject: Lift Station No. 2 Gravity Sewer Evaluation Tt #: 200-52528-12002 Date: June 15, 2012 1.0 INTRODUCTION The purpose of this evaluation is to investigate alternatives and make recommendations to resolve sewage backup problems at the 399 Holman Road residence. In addition, the memorandum analyzes the gravity sewer and lift station capacities to develop preliminary alternatives that will increase reliability of the collection system. 1.1 Background The general alignment of the gravity sewers, including Lift Station (LS) No. 9 and LS No. 2's northern and southern tributary (service) areas are depicted in Figure 1. LS No. 9 tributary area is the southernmost tributary area in the City's collection system and generally consists of multifamily condominiums. LS No. 9 is a duplex submersible type station and is located adjacent to Banana River Road. Wastewater from LS No. 9 is discharged, via a force main, to a manhole along Holman Road. The sanitary waste is then conveyed by gravity along Holman Road and through several private developments, including the Cape Shores Condominiums and the Cocoa Palms Mobile Home Park and ultimately discharges into LS No.2 on Center Street. Wastewater flow from LS No. 2 is pumped into the LS No. 1 gravity tributary area prior to repumping to the WWTP. This scope and evaluation focuses solely on LS No. 2's southern tributary area. No issues were reported in the northern tributary area of LS No. 2. Upon meeting with the City, the operations staff revealed that the primary problem with gravity sewer system occurs at a manhole adjacent the 399 Holman Road residence, the manhole that LS No. 9 discharges wastewater flow into. The residence at 399 Holman Road was constructed on a depressed plot where the home's finished floor elevation is 1.05 feet below the top of the manhole. When both pumps at LS No. 9 are operating continuously for a few minutes, the downstream manhole surcharges as a result of insufficient conveyance capacity in the gravity system. When the flow stages up in this manhole, the TETRATECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 2 residence at 399 Holman Road is at risk of sewage backing up into the gravity service line, and potentially into the home under worst case conditions. The City has rerouted the gravity service connection from the 399 Holman Road residence downstream of the LS No. 9 discharge manhole; however, the City is still concerned that backflow could occur under peak flow conditions. The City has mitigated backup potential in the gravity system by temporarily modifying LS No. 9, to only allow one (1) pump to operate at any time. The City's primary goal is to develop a cost effective solution to eliminate backup conditions at the Holman Road property. The City also has concerns about the hydraulic capacity of the gravity sewers in the LS No. 2 gravity sewer tributary area. Additional information was provided by the City or obtained from other sources for this review as follows: 1) General map of the City's sanitary sewer system (Figure 1) 2) LS No. 9 pump run times for the most current 12 month period. 3) Pump curves for LS No. 9 4) As -built drawings for LS No. 9 & LS No. 2 5) City of Cocoa water billing records for customers in the LS No.9 tributary areas under investigation for the most current 12 month period 6) Brevard County Property Appraiser land use information 7) Survey of 399 Holman Road property and MH 1, 2 and 3 For reference, the approximate hydraulic capacity of various size sewer lines based on minimum required slopes are presented in Table 1. The hydraulic capacities are for reference only. A survey including slope analysis of the entire tributary was not part of this assignment. It is assumed that the gravity sewers were constructed to minimum standards; however hydraulic capacities may vary based on actual slopes. TABLE 1 NOMINAL HYDRAULIC CAPACITY OF VARIOUS SEWER PIPES AT MINIMUM SLOPE (PER 10 STATE STANDARDS) MAssumes roughness factor of .Ol 3 (rough PVC) using Manning Equation. N TETRA TECH 2.0 EXISTING SYSTEM REVIEW Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 3 A review of the existing LS No. 9 and No. 2 tributary areas and capacities was conducted through the use of available "record" information as well as field inspections by Tetra Tech engineers. This section reviews the finding of the field inspections and lift station drawdown tests performed. In addition, the analysis reviews pump runtime data and number of residences in the tributary areas to estimate both the existing and required hydraulic capacity of the gravity system. Alternatives will be developed from these estimates. 2.1 Field Inspections Tetra Tech performed initial field inspections of the manholes, sewer inverts and diameters between LS No. 9 and LS No. 2 on March 19"' and April 23rd, 2012. The field data collected, including the invert depth, diameters and overall manhole depths along the gravity sewer route, is summarized in Figure 2. Additionally, Figure No. 2 includes manhole (MH) numbers that will be referenced throughout this evaluation. The uneven interior diameters of the gravity sewers are attributed to previous slip lining improvements. During field visits, it was visually observed that when LS No. 9 was operating (with only one pump), the manhole adjacent to the 399 Holman Road residence (MH No. 1) and the downstream manhole (MH No. 2) staged up approximately 12 inches above the invert. Also, the gravity sewer diameter exiting MH No. 1 was measured to be approximately 7.5 inches, while the gravity sewer diameter entering MH No. 2 was measured to be approximately 6 inches. The exact cause of the neckdown in the gravity main is unknown but it is suspected to be the reason for the wastewater staging up in the manholes. MH No. I and MH No. 2 were surveyed to detennine the slope of the gravity sewer, which was found to be approximately 0.4%. A slope of 0.4% is an acceptable minimum slope for an 8 -inch pipeline, but does not meet the required slope of a 6 -inch gravity sewer. 2.2 Lift Station No. 9 Drawdown and Runtimes The existing pumps at LS No. 9 are each rated for approximately 350 gpm, which was confirmed via on- site drawdown pump testing. At peak flows when both the lead and lag pumps are operating, the pumps are estimated to operate at approximately 420 gpm, which is in excess of the hydraulic capacity of a 6 - inch or 8 -inch gravity sewer at minimum slopes. The existing pump curves and the estimated system curve illustrating the pumping conditions described above are displayed in Figure 3. Tetra Tech also reviewed the pump run times over the last 12 months collected from LS No. 9. Table 2 summarizes some of the selected maximum runtimes for this time period. The values indicate that the peak daily flows are up to 88,200 gpd. In general, the average number of starts appears to be TETRATECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 4 approximately 40-60 per day and the average daily runtimes appear to be between 80 and 120 minutes per day, which is estimated to be a flow range of approximately 28,000 to 42,000 gpd. The number of starts and runtimes per day appear to be low in comparison to typical engineering standards, which indicates that the pumps are oversized. As mentioned previously the City personnel have modified the controls at LS No. 9 to only allow one pump to operate, the LS has been operating successfully in this arrangement for many months with no issues. TABLE 2 SUMMARY OF LS NO. 9 PEAK DAILY PUMPING EVENTS OVER THE LAST 12 MONTHS 2.3 5/16/2011 396* N/A* 6/26/2011 187 65,450 9/23/2011 184 64,400 9/24/2011 166 58,100 10/9/2011 203 71,050 10/10/2011 252 88,200 10/11/2011 232 81,200 10/12/2011 215 75,250 10/13/2011 197 68,950 10/14/2011 202 70,700 10/15/2011 175 61,250 10/30/2011 179 62,650 10/31/2011 212 74,200 11/1/2011 196 68,600 11/6/2011 176 61,600 11/7/2011 186 65,100 *Pump or time logging malfunction suspected Lift Station No. 9 Tributary Capacity Anal Additional data was collected pertaining to the size and quantity of existing condominium units that are located in the LS No. 9 tributary area to project wastewater flows. The number of units was established based on direct communication with management personnel from each condominium complex and information on the Brevard County Property Appraiser website. The LS No. 9 tributary area appears to be built out, thus no additional wastewater flows is expected in the future. TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 5 Projected wastewater flows were based on Florida Administrative Code (FAC) Chapter 64E wastewater generation rates and are summarized in Table 3. Tetra Tech also estimated potable water usage within the lift station tributary areas, as wastewater generation is typically between 70-80% of potable water usage. However the Chapter 64E generation estimates resulted in more conservative requirements and will be used for the evaluation. TABLE 3 WASTEWATER GENERATION BASED ON PROPERTY TYPE Table 4 illustrates the number of units and projected wastewater flows for each condominium in the LS No. 9 tributary area. The table, which calculates a conservative estimate of wastewater flows, indicates that the existing pumps could be replaced with smaller capacity pumps (approximately 203 gpm) while providing a level of service consistent with engineering standards. Reducing the capacity of the pumps would help reduce the amount of flow staging that occurs in the discharge manhole and other manholes in the LS No.2 southern tributary area, however staging would still occur where sections with diameters are smaller than 8—inches. TABLE 4 LIFT STATION NO. 9 WASTEWATER FLOW GENERATION ESTIMATE *Peak Hourly Flow to Average Daily Flow Factor of 4.0 used to estimate pumping capacity TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 6 2.4 Litt Station No. 2 Tributary Capacity Analysis Data was also gathered to estimate wastewater flow rates from the LS No. 2 southern tributary area (south of Center Street) to detennine the existing capacity of the gravity sewer. The flow generation calculations take into account the design discharge of LS No. 9 into the gravity sewer. The southern tributary area of LS Not was divided into five (5) zones as denoted in Figure 4. Wastewater from each zone can be cumulatively added to determine the estimate flow and gravity sewer requirements at the approximate termination of each zone. Table 5 displays the projected wastewater flows for the existing LS No. 2 tributary area per zone. Table 6 compiles the cumulative flows per zone based on the existing conditions and compares these flows to the both the required and existing gravity sewer diameters in each zone. The table indicates the capacity of gravity sewer system measured during Tetra Tech's inspections are undersized due to the LS No. 9 discharging into zone 1. If pumping capacities at LS No. 9 remain unchanged, the LS No.2 southern tributary gravity sewers should be increased to a minimum of 10 -inches in diameter at minimum slopes to avoid staging in the manholes. 2.5 Capacity Analysis Based on Build Out The southern tributary area for LS No. 2 is essentially at build out except for a large track in zone 2 at 6335 N Atlantic Ave. currently occupied by a miniature golf course and restaurant. Discussions with the City's staff have indicated that the construction of a hotel or condominium complex could potentially be constructed at the property. A search of the property indicated it was bn the market in 2010, but has since been taken off. The lot contains approximately 5.7 acres and can accommodate up to 171 hotel rooms, according to the 2010 real estate listing. If this lot was developed into a hotel or resort, the gravity system would connect to the existing gravity main between Holman Road and Cape Shores Drive. The existing gravity sewer is currently undersized in this area and cannot accommodate additional flow. The capacity improvement recommendations in Section 4.0 include provisions for the potential development of this parcel into a hotel or resort. TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 7 TABLE 5 LIFT STATION NO. 2 EXISTING WASTEWATER FLOW ESTIMATE (SOUTHERN TRIBUTARY) Notes: Unit counts estimated from Brevard County Property Appraiser website Peak Hourly Flow (PHF) to Average Daily Flow (ADF) factor of 4.0 used to estimate pumping capacity TABLE 6 LIFT STATION NO. 2 CUMULATIVE WASTEWATER FLOWS (SOUTHERN TRIBUTARY) AND GRAVITY SEWER REQUIREMENTS (1)Depth of manholes prevented accurate measurement of gravity sewers. TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 8 3.0 ALTERNATIVES TO ELIMINATE BACKUPS This section will summarize the analyses recommended to prevent staging and eliminate backups into the Holman Road property. The results of the investigation appear to establish three (3) potential alternatives for preventing backflow to the Holman Road residence: 1. Possible relocation of force main discharge to west side of North Atlantic Avenue (AIA) to bypass LS No. 2 tributary area and pump directly to LS No. 1 tributary area. 2. Install a private lift station at or nearby the 399 Holman Road residence to prevent sewage backflow. �s t 3. Install a gravity service line from 399 Holman Road to LS No. 9, sized for future conditions if the v,s I�E 'r OP'T nearby vacant property at 6101 N. Atlantic Ave. is commercially developed. �—. v-► A S 5� 3.1 Alternative 1: Force Main Relocation Construction of a force main to discharge wastewater from LS No. 9 to LS No. l's tributary system and bypass of LS No. 2 tributary area requires approximately 3,600 linear feet of force main along with significant improvements to the gravity sewers in the LS No. 1 tributary area. Over 2,500 linear feet of force main would need to be constructed in the congested right-of-way of A I A. This alternative does not eliminate the potential for a backup; a blockage in a downstream gravity sewer could result in staging of the upstream manholes and a backup at the residence. Analysis revealed this alternative is not feasible due to the overall cost, constructability issues and incomplete elimination of backups. 3.2 Alternative 2: Private Lift Station Installation of a private lift station that would solely serve the 399 Holman residences would eliminate the risk of backup currently experienced. The lift station construction would likely be a small duplex grinder station similar to those already installed for residences along the Intercoastal waterway. It is likely that the lift station could be installed near the property along the south or west side of Holman Road and discharge into the same manhole adjacent to the residence (MH No. 1). An easement may be required for this option and the City may be compelled to maintain the LS to appease the resident's concerns. Installing a pump station for the 399 Holman Road residence eliminates the potential sewage backup at the -residence, but will not reduce the staging in the manholes. Figure 5 presents a preliminary depiction of this option. TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 9 A preliminary cost estimate of $37,485.00 has been estimated for Alternative No. 2. A line item breakdown of the cost estimate is located in Table 7. These costs are budgetary in nature and would require additional development during preliminary design. For all alternatives, the cost of acquiring easements has not been included in the estimate, but could be required. TABLE 7 BACKUP ELIMINATION ALTERNATIVE NO. 2 — PRIVATE LIFT STATION PRELIMINARY OPINION OF PROBABLE COST 3.3 Alternative 3: Gravity Service to LS No. 9 Gravity sewer installation to redirect the sanitary service from the 399 Holman Road residence to the LS No. 9 wet well will remove the connection to the LS No. 2 gravity tributary area and eliminate the potential for backups. This alternative involves the construction of approximately 750 feet of gravity sewer to route flow back to LS No. 9. Although there is a slightly closer manhole just south of the pool at the Hidden Harbor Condominiums, the manhole appears to be too shallow to direct the sanitary flow at minimum slopes. Based on property appraiser's maps, it appears that there is right-of-way along Banana River Road to construct the gravity sewer. A private residence at 6101 N. Atlantic Ave. would need to be crossed, which would require the acquisition of an easement if the existing easement is not wide enough to construct the new gravity sewer line. Preliminary calculations indicate that a 4 -inch gravity pipeline installed at a slope of 1.0% to maintain a minimum velocity in the pipeline would provide sufficient capacity for the 399 Holman Road residence. However, the City's operational staff indicated that N TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 10 installing an 8 -inch line would be beneficial if any future development occurs at 6101 N. Atlantic Avenue property, which is currently vacant and is partially zoned for commercial use. Rerouting the gravity service from 399 Holman Road to LS No. 9 eliminates the potential sewage backup at the residence, but will not reduce the staging in the manholes, resulting from the limited hydraulic capacity of the existing gravity sewers. Figure 6 presents a preliminary depiction of Alternative 3. A preliminary cost of $92,978.00 has been estimated for Alternative No. 3. A line item breakdown of the cost estimate is located in Table 8. These costs are budgetary in nature and would require additional development during preliminary design. TABLE 8 BACKUP ELIMINATION ALTERNATIVE 3 — REROUTE GRAVITY SERVICE TO LS NO. 9 PRELIMINARY OPINION OF PROBABLE COST 3.4 Backup Elimination Summary Alternatives No. 2 and No. 3 presented above are viable options to alleviate the backup issues experienced at 399 Holman Road. Backup elimination Alternative No. 3 features a moderate cost, is constructible with minimal impacts to the surrounding community, allows for future connections along Holman Road and provides a negligible maintenance increase for the City and is the preferred alternative. However, implementation of Alternative No. 3 alone will not address the root cause of insufficient capacity of the gravity sewers in the LS No. 2 southern tributary area. Without increasing the capacity of the system, staging problems will continue and could result in sanitary sewer overflows in other areas of TETRATECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 11 the system. The following sections will investigate the deficiencies in the LS No. 2 southern tributary area and provide recommendations to increase reliability of the system. 4.0 CAPACITY IMPROVEMENTS FOR LS NO. 2 SOUTH TRIBUTARY AREA As indicated in Section 2.0, the LS No. 2 southern tributary system is currently undersized based on current estimates. It is recommended that improvements to increase the hydraulic capacity be implemented. The section investigates reduction of pumping capacity at LS No. 9 and increases in gravity sewer size to increase the hydraulic capacity in the tributary area, along with budgetary costs and a review of construction methods. 4.1 Reduced Pumping Capacity at LS No. 9 The provided runtime and pump start data, in conjunction with the build out wastewater generation calculations in the LS No. 9 tributary area, indicate a reduction in pump capacity at LS No. 9 is possible. The reduction results in a smaller diameter requirement of the gravity sewers throughout the tributary area. Table 9 indicates that zones 1, 2, and 3 require gravity sewer diameter of 8 -inch, while zones 4 and 5 require 10 -inch diameter, based on existing generation rates and reduced pumping capacities at LS No. 9. However, these capacity improvements do not account for the potential future development at 6335 N Atlantic Ave located in zone 2. Improvements to gravity sewers would be required in zones 2, 3, 4 and 5 if the property was developed into a hotel or resort. TABLE 9 LIFT STATION NO. 2 CUMULATIVE WASTEWATER FLOWS (SOUTHERN PORTION) WITH REDUCED LS NO. 9 PUMPING CAPACITIES ANDGRAVITY SEWER REQUIREMENTS (')From previous tables. TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 12 4.2 Gravity Sewer Improvements To accommodate the proposed development, Tetra Tech analyzed the available capacity if zones 2, 3, 4 and 5 were upsized one pipe diameter from the values listed in Table 9. Based on the analysis, upsizing gravity sewers one pipe diameter results in an available future hydraulic capacity of 100 gpm (36,000 gpd), allowing accommodation of a 180 room hotel or resort. Table 10 presents the estimated peak cumulative wastewater flows per zone and required future gravity sewer requirements to accommodate the estimated build out condition. It should be noted the flow estimates are based on minimum slope requirements of the gravity sewers. If additional slopes can be achieved during the design phase, the gravity sewer diameter requirements could decrease; however, additional investigation and survey are required to accurately determine the slopes. The future development at 6335 N Atlantic Ave., includes a 5.7 acre lot that fronts to N. Atlantic Ave. As previously stated, a 2010 real estate listing the property can accommodate up to 171 hotel rooms. The future development assumption only include this 5.7 acre parcel, however, if a developer acquired the three residential properties along the intercoastal, a potential waterfront resort of greater than 10 acres could be constructed. The acquisition and rezoning requirements make this option improbable; and was not included in the analysis. Figure 7 presents a preliminary depiction of the capacity improvements. These improvements minimize gravity sewer diameters while accommodating for future development in zone 2. TABLE 10 LIFT STATION NO. 2 CUMULATIVE WASTEWATER FLOWS INCLUDING REDUCED LS NO.9 PUMPING AND FUTURE DEVELOPMEN AND GRAVITY SEWER REQUIREMENTS (')From previous tables. TETRA TECH 4.3 Construction Methods Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 13 Based on the preliminary inspection and capacity analysis, the gravity system could require up to 4,000 linear feet of gravity main replacement. The effort to complete this work would be substantial and may need to be addressed as part of a 5 year capital improvement plan (CIP). Completion of these capacity improvements would reduce manhole staging and provide a high level of service for all existing and future customers in the LS No. 2 southern tributary area. It is likely that a combination of conventional replacement and pipe bursting would be used for the sewer improvements. The first replacement option, conventional removal and replacement, involves bypass pumping, excavation of the existing pipelines, removal and replacement of the existing pipe, backfilling, and restoration of areas disturbed by the construction activities. The second replacement option, pipe bursting, involves using a trenchless technology that is somewhat similar to directional drilling, however, the existing pipe is used to provide a "pilot conduit" for bursting equipment. Pipe bursting technologies allow for increase of pipe size up to two diameters greater than the current gravity sewer diameter. This equipment breaks the existing pipe and pushes it into the surrounding soil to make room for the new pipe that is pulled through the larger opening. In cases where there is minimal cover over an existing pipe, the bursting process often results in "heaving" of the ground surface. Existing service laterals must be excavated and connected to the new pipe after the bursting and pulling operations are complete. Open trench methods are more cost effective in areas of open space or unpaved roadways. Pipe bursting is more cost effective in congested areas or deep gravity sewers, where restoration is more extensive. 4.4 Preliminary Costs A preliminary cost estimate for the capacity improvements described above are $927,927.00, a line item breakdown is presented in Table 11. Estimated costs for the capacity improvements are conservative and assume replacement of gravity sewers in all zones. However, actual mains to be replace should be based on a complete survey and inspection of the tributary area, as the size gravity sewer in zone 4 was not field verified and may not require replacement. A contingency has been added to the total cost pending an additional investigation to more accurately determine the magnitude of the improvements needed. TETRA TECH Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 14 TABLE 11 CAPACITY IMPROVEMENTS IN LS NO.2 SOUTHERN TRIBUTARY AREA PRELIMINARY OPINION OF PROBABLE COST 1. Assumed half existing manholes require replacement 2. Additional contingency pending full review of system TETRATECH 5.0 SUMMARY AND CONCLUSIONS Mr. Jeff Ratliff Cape Canaveral Utilities June 15, 2012 Page 15 Based on this evaluation, it is recommended that one of the backup elimination alternatives be selected initially to alleviate backflow problems in a timely manner, so that capacity improvements could be constructed in phases with a longer term capital improvements plan. Backup elimination alternative No. 2 and No. 3 are feasible options for preventing backup to the 399 Holman Road residence. Backup elimination Alternative No. 3 has the benefits of reduced maintenance and capacity for future connections along Holman Road; however, the Alternative will not address the root cause of insufficient capacity in the LS No. 2 southern tributary area. Without increasing the capacity of the system, staging problems could continue and result in sanitary sewer overflows in other areas of the system. Therefore, it is recommended the City implement the outlined capacity improvements to address the deficiencies in the existing gravity system and allow for future build out conditions in LS No. 2 southern tributary area. Additional investigations are required to detennine the exact length and size of the gravity main improvements; however it is expected that the construction would require the installation of between 2,500 to 4,000 linear feet of gravity sewer, by conventional removal/replacement and pipe bursting techniques, depending on the location and slope of the existing gravity sewer. In summary, it is recommended that the City route flow from the Holman property directly to LS No. 9, reduce the pump size at LS No. 9, and implement the hydraulic capacity improvements in the LS No. 2 southern tributary area. End of Memorandum. 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Box 1086 Cape Canaveral, Florida 32920-1086 (321) 453-0429 emcmillinid0yahoo.com 21 February 2015 Chairperson Avro Eilau Board of Adjustment 550 Jackson Avenue Cape Canaveral, Florida 32920 Re: Cumberland Farms Dear Chairperson Eilau: Permit me to bring to your attention a critical aspect of the Cumberland Farms project to build a convenience store/gas station on U.S. Highway A1A. Attached is a June 15, 2012 study prepared for the City by Tetra Tech examining the sewer system from Lift Station (L.S.) No. 9 to L.S. No. 2. This is the sewer which serves the Dollar General store and which will serve the Cumberland Farms facility. The study is clear that the sewer is inadequate. It was inadequate before Dollar General built its store and is even more inadequate because of the Dollar General store. "The existing gravity sewer is currently undersized in this area and cannot accommodate additional flow." Tetra Tech, Page 6. Also enclosed are photos of raw sewage gushing to the surface at the Hartley residence at 399 Holman Road and flowing down the driveway leading to the Marino residence. Permitting these developments to hook up to a sanitary sewer that the City knows is inadequate is contrary to the Comprehensive Plan: "GOAL The overall goal for this sub -element is provision of sanitary sewer facilities to meet the needs of the existing and future citizens of Cape Canaveral." "SS -1: Assure that all existing and future inhabitants and businesses in the City have access to State -approved, properly functioning sanitary sewer facilities during the 5- to 10 -year time -frame of this Plan by correcting existing deficiencies and making sure facilities meet future needs." -I- These issues of inadequate sewer capacity, the Comprehensive Plan and the threat posed to existing residences by the Cumberland Farms project were not pointed out to the Planning & Zoning Board. Until the City improves the sewer system, no further developments which place added demand on the sewer system in the area examined by Tetra Tech should be permitted. As an individual who served on the Board of Adjustment for many years, both as a Member and as Chairperson, I can appreciate the pressures that are sometimes felt. The guiding star is to take the steps that are legal and proper. I am hopeful that you and your colleagues will do so. Cc: City Manager Assistant City Attorney Attorney Philip Nohrr Attorney Ralf Brookes Mr. Charles Hartley Very truly yours, G jrL ;� ` •2 -2- Earl McMillin McMillin Earl McMillin P.O. Box 1086 Cape Canaveral, Florida 32920-1086 (321) 453-0429 emcmillinidPyahoo.com 21 February 2015 Mr. David L. Greene City Manager City of Cape Canaveral P.O. Box 326 Cape Canaveral, Florida 32920-0326 Re: Cumberland Farms Dear Mr. Greene: Enclosed is a copy of a letter, together with enclosures, that I have sent to each individual on the Board of Adjustment. This same material has been sent to Attorney Anthony Garganese, to Attorney Philip Nohrr and to Attorney Ralf Brookes. Although we do own a property in the city, at this time my wife and I do not reside in Cape Canaveral. However, my son and his family reside at 397 Holman Road. It is on behalf of my son and his family that I have taken this step. Very truly yours, Earl McMillin Earl McMillin P.O. Box 1086 Cape Canaveral, Florida 32920-1086 (321) 453-0429 eincmillinjd(@yahoo.com 21 February 2015 Chairperson Avro Eilau Board of Adjustment 550 Jackson Avenue Cape Canaveral, Florida 32920 Re: Cumberland Farms Dear Chairperson Eilau: 9 Permit me to bring to your attention a critical aspect of the Cumberland Farms project to build a convenience store/gas station on U.S. Highway AIA. Attached is a June 15, 2012 study prepared for the City by Tetra Tech examining the sewer system from Lift Station (L.S.) No. 9 to L.S. No. 2. This is the sewer which serves the Dollar General store and which will serve the Cumberland Farms facility. The study is clear that the sewer is inadequate. It was inadequate before Dollar General built its store and is even more inadequate because of the Dollar General store. "The existing gravity sewer is currently undersized in this area and cannot accommodate additional flow." Tetra Tech, Page 6. Also enclosed are photos of raw sewage gushing to the surface at the Hartley residence at 399 Holman Road and flowing down the driveway leading to the Marino residence. Permitting these developments to hook up to a sanitary sewer that the City knows is inadequate is contrary to the Comprehensive Plan: "GOAL The overall goal for this sub -element is provision of sanitary sewer facilities to meet the needs of the existing and future citizens of Cape Canaveral." "SS -1: Assure that all existing and future inhabitants and businesses in the City have access to State -approved, properly functioning sanitary sewer facilities during the 5- to 10 -year time -frame of this Plan by correcting existing deficiencies and making sure facilities meet future needs." -I- These issues of inadequate sewer capacity, the Comprehensive Plan and the threat posed to existing residences by the Cumberland Farms project were not pointed out to the Planning & Zoning Board. Until the City improves the sewer system, no further developments which place added demand on the sewer system in the area ermined by Tetra Tech should be permitted. As an individual who served on the Board of Adjustment for many years, both as a Member and as Chairperson, I can appreciate the pressures that are sometimes felt. The guiding star is to take the steps that are legal and proper. I am hopeful that you and your colleagues will do so. Cc: City Manager Assistant City Attorney Attorney Philip Nohrr Attorney Ralf Brookes Mr. Charles Hartley -2- Very truly yours, Earl McMillin Sewage Gusher ---Southside Hartley Residence ---399 Holman Road. Ajft- Ah fl 4i Sewage Gusher---Southside Hartley Residence---399 Holman Road. 0 Sewage Flowing Down Marino Driveway. F -0F,' SCANNING MAR `_' ] 20111 24-37-26-00-251 VARS PARS NOW 00-251, 286, 287 -r1k)fl 1 -0 22 1 23 BEFORE MAP 16dOFtIoW LTISOFLT s C22&S40'OF�i 4S3N160'OFLT1SEC26 -S WOF ST RDN 254311090 8 648d3.TA9)EXC 3161127011933 4028/1648 BUT EXCEPTINGXCEPTIONS40241844 6) - ----------------�,, za 253 / S 200' OF 360' OF SECS 26827 W OF ST RD / C 51912158 8 5460/3387 i- 264.2 i L2TSRD 5 PTOF E3WOF 62WOF 1 ' OF SECS 26. 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